commit 
94bef000f1d4aa111f4ddda1482cf3b30ad069ce upstream.
Shifting sensor data to the right 2 bits was incorrect and caused the
scaling values + offsets to be invalid.
Reported-by: Alison Schofield <amsfield22@gmail.com>
Signed-off-by: Matt Ranostay <mranostay@gmail.com>
Tested-by: Alison Schofield <amsfield22@gmail.com>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
                dev_err(&client->dev, "cannot read high byte measurement");
                return ret;
        }
-       val = ret << 6;
+       val = ret << 8;
 
        ret = i2c_smbus_read_byte(client);
        if (ret < 0) {
                dev_err(&client->dev, "cannot read low byte measurement");
                return ret;
        }
-       val |= ret >> 2;
+       val |= ret;
 
        return val;
 }
        case IIO_CHAN_INFO_SCALE:
                if (chan->type == IIO_TEMP) {
                        *val = 165000;
-                       *val2 = 65536 >> 2;
+                       *val2 = 65536;
                        return IIO_VAL_FRACTIONAL;
                } else {
-                       *val = 0;
-                       *val2 = 10000;
-                       return IIO_VAL_INT_PLUS_MICRO;
+                       *val = 100;
+                       *val2 = 65536;
+                       return IIO_VAL_FRACTIONAL;
                }
                break;
        case IIO_CHAN_INFO_OFFSET:
-               *val = -3971;
-               *val2 = 879096;
+               *val = -15887;
+               *val2 = 515151;
                return IIO_VAL_INT_PLUS_MICRO;
        default:
                return -EINVAL;